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PORTLAND, Ore. (KOIN) – The head of the National Transportation Safety Board is blaming systemic failures for a door plug blowout in the skies over Portland, Oregon, in January 2024.

Alaska Airlines Flight 1282 made an emergency landing 30 minutes after taking off from Portland International Airport when the door plug separated from the aircraft at 14,830 feet, leaving a hole in the side of the plane. Oxygen masks dropped during the rapid decompression and objects were sucked out of the hole as the passengers and crew contended with wind and roaring noise.

All passengers survived, but several suffered minor injuries.

A 17-month investigation by the NTSB has determined that the four bolts meant to hold the door plug in place were removed during a repair job, and never replaced.

Investigators determined the door plug had also gradually moved during the 154 flights prior to this incident, before it ultimately flew off.

  • FILE - This image taken Sunday, Jan. 7, 2024, and released by the National Transportation Safety Board, shows the section of a a Boeing 737 Max where a door plug fell while Alaska Airlines Flight 1282 was in flight. (NTSB via AP, File)
  • FILE - The door plug from the Alaska Airlines Flight 1282's Boeing 737-9 MAX airplane is shown at the National Transportation Safety Board laboratory, in Washington, July 30, 2024. On Tuesday, August 6, 2024, the National Transportation Safety Board opens a two-day hearing on the blowout of the door plug from the Alaska Airlines flight traveling 16,000 feet above Oregon. (AP Photo/Manuel Balce Ceneta, File)
  • This photo released by the National Transportation Safety Board shows an opening in the fuselage where a door plug fell from Alaska Airlines Flight 1282, on Jan. 7, 2024, in Portland, Ore. (National Transportation Safety Board via AP, File)
  • The door plug from the Alaska Airlines Flight 1282's Boeing 737-9 MAX airplane is shown at the National Transportation Safety Board laboratory, in Washington, Tuesday, July 30, 2024. The door plug is showing some signs of wearing out, scratches caused by rubbing against hard surfaces and a gap on the top section above the window (front bottom of the picture). (AP Photo/Manuel Balce Ceneta)

“The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA,” NTSB Chair Jennifer Homendy said. “This time it was missing bolts securing the door plug, but the same safety deficiencies that led to this accident could just have easily led to other manufacturing quality escapes and other accidents.”

Boeing factory workers told NTSB investigators they felt pressured to work too fast and were asked to perform jobs they weren’t qualified for. None of the 24 people on the door team were ever trained to remove a door plug before working on the plane in question, and only one of them had ever done so before. That person was on vacation when the repair was being done.

The NTSB says Boeing and the Federal Aviation Administration have improved training and processes since the blowout.

Boeing and Spirit AeroSystems — the company that made and installed the door plug — are redesigning them with another backup system to keep the panels in place even if the bolts are missing, but that improvement isn’t likely to be certified by the FAA until 2026 at the soonest. The NTSB urged the companies and the regulator to make sure every 737 Max is retrofitted with those new panels.

In a statement, Boeing said that they “regret this accident and continue to work on strengthening safety and quality across our operations.”

“We will review the final report and recommendations as we continue to implement improvements.”

The Associated Press contributed to this story.

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